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某水利枢纽3#冲沙闸裂缝状态闸室稳定性研究
引用本文:李昌永.某水利枢纽3#冲沙闸裂缝状态闸室稳定性研究[J].中国农村水利水电,2010,0(1):82-87.
作者姓名:李昌永
作者单位:水利部新疆水利水电勘测设计研究院勘测总队,新疆,昌吉,831100
摘    要:草街水利枢纽冲沙闸在施工期发现在底板部位和冲沙闸墩体不同部位出现不同数量和规模的裂缝,其中底板存在横向贯通性裂缝。为了解裂缝对结构性能降低程度和为裂缝修复加固设计提供依据,设计了完整状态、裂缝存在状态和裂缝修复状态的冲沙闸完建期、2个正常蓄水和3个检修等18个工况,经计算分析,发现:各冲沙闸裂缝状态闸室整体稳定性不满足规范要求,需要进行了加固,加固标准为裂缝区混凝土强度的85%,实际加固施工控制标准为上述强度阈值的1.5倍。

关 键 词:冲沙闸,裂缝,稳定性,裂缝修复

Study on No.3 Flushing Sluice's Stability of Certain Key Water Control Project Under Cracking Condition
LI Chang-yong.Study on No.3 Flushing Sluice's Stability of Certain Key Water Control Project Under Cracking Condition[J].China Rural Water and Hydropower,2010,0(1):82-87.
Authors:LI Chang-yong
Institution:LI Chang-yong(Geotechnical Engineering Company of Xinjiang Hydroelectric Investigation & Design Institute Ministry of Water Resources,Changji 831100,China)
Abstract:There exist different quantity and scale crack in the bottom and body of the flushing sluice of caojie key water control project during the construction period,cracks in the bottom being horizontally traversed.To know the reducing degree of the structural peformance affetced by the crack and to provide basis for the crack restored and reinforced,the eighteen comouting schemes such as construction,normal.water and overhauling under good working,crack existed and crack restored conditions are designed.Found t...
Keywords:flushing sluice  crack  stability  crack modification  
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