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气吸滚筒式花生穴播器投种性能分析与试验
引用本文:康建明,向阳,张春艳,彭强吉,张国海,张宁宁,王小瑜,唐朝辉.气吸滚筒式花生穴播器投种性能分析与试验[J].农业工程学报,2022,38(14):1-11.
作者姓名:康建明  向阳  张春艳  彭强吉  张国海  张宁宁  王小瑜  唐朝辉
作者单位:1. 山东省农业机械科学研究院,济南 250100;2. 山东理工大学农业工程与食品科学学院,淄博 255000;1. 山东省农业机械科学研究院,济南 250100;3. 农业农村部黄淮海现代农业装备重点实验室,济南 250100;;4. 山东省农业科学院,济南 250100
基金项目:国家重点研发计划项目(2020YFD1000902);山东省重大科技创新工程项目(2019JZZY010702);山东省自然科学基金青年项目(ZR2021QC163)
摘    要:针对气吸滚筒式花生穴播器投种过程中种子不能准确落入导种机构而造成漏播、重播的问题,该研究提出了一种通过调整穴播器盖边缘开口位置和导种机构安装角度的方法寻求最佳投种轨迹,对种子脱离穴播器盖进入导种机构阶段建立动力学模型,明确了投种轨迹变化机理,确定了穴播器盖和导种机构的安装参数。借助EDEM仿真软件研究了穴播器盖和导种机构在不同安装角度下的投种性能,得出种子在与分种盘挡片接触状态下脱离穴播器盖边缘的投种性能最佳。选取穴播器盖安装角度、导种机构安装角度和机具前进速度为试验因素,以排种粒距合格率、漏播率、重播率为试验指标,在排种试验台上进行三因素三水平组合试验。结果表明:在穴播器盖安装角为17.10°、导种机构安装角为11.18°、机具前进速度为3.85 km/h的条件下投种性能最优,此时排种粒距合格率为95.37%。田间试验结果表明,调节穴播器盖安装角为17.10°、导种机构安装角11.18°,机具前进速度在3.05~4.65 km/h范围内,试验结果与台架试验结果基本相符,排种粒距合格率大于89%、漏播率小于7%,重播率小于5%,满足花生单粒精量播种要求。

关 键 词:农业机械  试验  种子  花生  气吸式穴播器  投种性能
收稿时间:2022/4/6 0:00:00
修稿时间:2022/7/9 0:00:00

Analysis and experiments of the seed feeding performance of air-suction roller dibbler for peanuts
Kang Jianming,Xiang Yang,Zhang Chunyan,Peng Qiangji,Zhang Guohai,Zhang Ningning,Wang Xiaoyu,Tang Chaohui.Analysis and experiments of the seed feeding performance of air-suction roller dibbler for peanuts[J].Transactions of the Chinese Society of Agricultural Engineering,2022,38(14):1-11.
Authors:Kang Jianming  Xiang Yang  Zhang Chunyan  Peng Qiangji  Zhang Guohai  Zhang Ningning  Wang Xiaoyu  Tang Chaohui
Institution:1. Shandong Academy of Agricultural Machinery, Jinan 250100, China; 2. College of Agricultural Engineering and Food Science, Shandong University of Technology, Zibo 255000, China;;1. Shandong Academy of Agricultural Machinery, Jinan 250100, China; 3. Huang Huai Hai Key Laboratory of Modern Agricultural Equipment, Ministry of Agriculture and Rural Affairs, Jinan 250100, China;; 4. Shandong Academy of Agricultural Sciences, Jinan 250100, China
Abstract:Abstract: An air-suction drum-type dibbler has been widely used for peanut seed feeding in recent years. However, the seeds cannot accurately fall into the seed guiding mechanism, due to the missed sowing and rebroadcast in the dibbler. In this study, the seed feeding trajectory was optimized to adjust the opening position of the cover edge in the dibbler and the installation angle of the seed guiding mechanism. A dynamic model was also established to clarify the variation in the seed feeding trajectory for the stage when the seeds left the cover of the dibbler to enter the seed guiding mechanism. The seeding performance of the dibbler cover and the seed guiding mechanism was then optimized to determine the installation angles using EDEM software. The best seeding performance was achieved in the contact with the seed stopper of the seed separation tray when the seed was separated from the edge of the dibbler cover. A three-factor and three-level combination test was carried out on the seed metering test bed. Among them, the test factors were the installation angle of the dibbler cover and the seed guiding mechanism, as well as the forward speed of the machine, while the qualified rate of the seed spacing, the missed seeding rate, and the rebroadcast rate were taken as the test indicators. The results showed that the best seeding performance was achieved, where the installation angles of the dibbler cover and the seed guiding mechanism were 17.10° and 11.18°, respectively, while the working speed of the machine was 3.85 km/h. Correspondingly, the qualified rate of seed spacing was 95.37% during this time. A reasonable range of installation parameters was determined, according to the influence of the installation angle of the dibbler cover and seed guiding mechanism on the seeding trajectory. Specifically, the larger the installation angle of the dibbler cover was, the more stable the seed cover separation process was; The smaller the installation angle of the seed guiding mechanism was, the easier the seeds fell into the effective area of the seed guiding mechanism. Therefore, the comparison test was then performed on the installation angle of the dibbler cover and seed guiding mechanism of 20° and 10°, respectively. It was found that the seeding performance of the optimal installation combination was significantly improved than that of the installation combined with the installation angle of the dibbler cover of 20° and the installation angle of the seed guiding mechanism of 10° under the forward speed of 3.00-5.00 km/h. More importantly, there was a more significant seeding performance in the optimized dibbler, particularly with the acceleration of the forward speed of the machine. Huayu 25 peanut seeds were selected to verify in the field experiment. Once the standby speed was stable, the length of the single ridge was counted as the planting in two rows within 15 m. Each experiment was repeated three times. There was flat and light sandy soil terrain in the experimental field, where the soil moisture content was 13%-15%. The field tests showed that the optimal adaptability was achieved to adjust the installation angle of the dibbler cover to 17.10°, the installation angle of the seed guiding mechanism to 11.18°, while the forward speed of the machine and tool within the range of 3.05-4.65 km/h. The qualified rate of seed spacing was greater than 89%, whereas, the missed sowing rate and rebroadcast were less than 7%, and 5%, respectively, fully meeting the requirements of precision sowing of a single peanut.
Keywords:agricultural machinery  experiments  seeds  peanut  air-suction roller dibbler  seeding performance
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