首页 | 本学科首页   官方微博 | 高级检索  
     检索      

参窝水库溢流坝闸墩裂缝加固处理效果分析
引用本文:梁力,夏海江,王健,杨毅.参窝水库溢流坝闸墩裂缝加固处理效果分析[J].现代农业科技,2014(3).
作者姓名:梁力  夏海江  王健  杨毅
作者单位:东北大学资源与土木工程学院;辽宁省水利水电科学研究院;
摘    要:参窝水库运行以来,溢流坝闸墩出现竖向活动裂缝,危及结构安全,提出适宜的修补加固技术,并对修补加固处理后的结构采用ANSYS软件进行受力状态有限元计算分析,得出闸墩混凝土裂缝修补加固后安全可靠,裂缝不再继续扩展,工程可安全运行,继续发挥其效益。

关 键 词:溢流坝闸墩  裂缝  修补加固  效果  参窝水库

Strengthening Effect Analysis of Sluice Pier Cracks in Shenwo Reservoir Overflow Dam
Abstract:Vertical lively cracks on sluice pier in Shenwo Resevoir overflow dam were appeared since operation, and the structural safety of dam was endangered.Suitable technology of repairing and strengthening were proposed,then structurarl stress state of finite element computational analysis were conducted by using ANSYS software after repairing and strengthening.The results concluded that the piers were safity after repairing and strengthening for concrete crack,cracks no longer continue to expanded,and the safe operation of the project could be continued to play its role.
Keywords:sluice pier in overflow dam  cracks  repair and reinforcement  effect  Shenwo Reservoir
本文献已被 CNKI 等数据库收录!
设为首页 | 免责声明 | 关于勤云 | 加入收藏

Copyright©北京勤云科技发展有限公司  京ICP备09084417号